by randyswelding » Mon Jan 25, 2010 7:16 pm
well i found part of the reason,the return T was a little loose so i tightened that and its still takes a little bite of time to start but not as bad as it was before so im still in the search,but i did make 334hp/820tq with 1/8 bump timin and 348hp/822tq with the ksb switch on so i got a leak somewhere.
'92 D350 cab and chassy,pump turned up with 1/8 timin,coaltriann 6x16 sticks,htt manifold,asa intake cooler tubez,south bend 13" clutch rebuilt G360,ps cooler,industrial super 62 phat shaft turbo,weldin bed.
12 Chevy 3500ltz lifted, deleted, and bed with sae 300 ss hood for new rig